引用本文:曾凡平,田广新. 液化天然气工厂重烃脱除工艺方案比选[J]. 石油与天然气化工, 2015, 44(1): 35-38.
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液化天然气工厂重烃脱除工艺方案比选
曾凡平,田广新
华油天然气股份有限公司
摘要:
分析了液化天然气工厂重烃脱除的现状及存在的问题,对比了多种重烃脱除方案的优劣性。以华油天然气股份有限公司处理规模为100×104 m3/d(20 ℃,101.325 kPa)的广元LNG工厂现有装置为例,在脱水单元后新增1套脱重烃装置可取得良好的重烃脱除效果,减少重烃闪蒸气量,提高天然气液化率,降低LNG产品的比功耗,促进装置长周期满负荷稳定运行。
关键词:  液化天然气  重烃脱除  变温吸附  工艺改造  节能降耗
DOI:10.3969/j.issn.1007-3426.2015.01.008
分类号:TE644
基金项目:四川省教育厅重点项目“LNG加气站、气化站、储备库的BOG再液化工艺研究”(13ZA0175)。
Scheme comparison and selection of heavy hydrocarbon removal process in LNG plant
Zeng Fanping, Tian Guangxin
(China Natural Gas Corporation Limited, Chengdu 610100, China)
Abstract:
Current situation and existing problem of heavy hydrocarbon removal process in the LNG plant were analyzed. Taking the existing devices in Guangyuan LNG plant of China Natural Gas Corporation Limited as example, the processing capacity of which was 1 000×103 m3/d(at 20 ℃ and 101.325 kPa), it is helpful to improve the effect of heavy hydrocarbon removal by adding a new adsorption equipment following the dehydration unit. Meanwhile, it can reduce the flow rate of flash gas, increase the liquefaction ratio of the natural gas, and decrease the unit energy consumption, as well as promote keeping the plant for a long-term and stable full load operation.
Key words:  liquefied natural gas  heavy hydrocarbon removal  temperature swing adsorption  technical transformation  energy conservation