引用本文:白丹江,蔡明件,谢会. 硫磺回收装置烟气排放超标原因分析及对策[J]. 石油与天然气化工, 2019, 48(1): 18-25, 31.
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硫磺回收装置烟气排放超标原因分析及对策
白丹江1,蔡明件2,谢会2
1.金澳科技(湖北)化工有限公司;2.上海河图工程股份有限公司武汉分公司
摘要:
分析了金澳科技(湖北)化工有限公司2×104 t/a硫磺回收装置排放烟气中SO2含量超标的原因,并采取了相应的改造措施,主要包括:①将液硫池废气由尾气炉改至燃烧炉;②更换更高效的脱硫溶剂;③更换有机硫水解能力更强的催化剂;④在尾气吸收塔后串联1台尾气碱洗塔。在实施①②③及优化工艺参数的前提下,排放烟气中SO2质量浓度小于100 mg/m3。 
关键词:  硫磺回收  达标排放  原因分析  治理措施  保护环境
DOI:10.3969/j.issn.1007-3426.2019.01.004
分类号:
基金项目:
Cause analysis and countermeasures of discharged flue gas of sulfur recovery unit exceeding standard
Bai Danjiang1, Cai Mingjian2, Xie Hui2
1. Kingao (Hubei) Science & Technology Chemical Industry Co., Ltd., Qianjiang, Hubei, China;2. Shanghai Hoto Engineering Inc.Wuhan Branch Office, Shanghai, China
Abstract:
This paper analyzed the reasons for exceeding standard of sulfur dioxide mass concentration in discharged flue gas from 20×103 t/a sulfur recovery unit of Kingao (Hubei) Science & Technology Chemical Industry Co., Ltd. Corresponding revamping measures were adopted, which included:(1) Introducing the off gas from liquid sulfur tank to the combustion furnace; (2) using desulfurization solvent with better desulfurization performance; (3) using catalysts with better organic sulfur hydrolysis ability; (4) adding a caustic wash tower cascaded to the tail gas absorber. After implementing the former measures (1)(2)(3) and adjusting the local process parameters, the SO2 mass concentration in discharged flue gas was less than 100 mg/m3.
Key words:  sulfur recovery  up-to-standard emission  cause analysis  control measure  protect environment